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Wampus_cat

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Posts posted by Wampus_cat


  1. So... upon further testing I seem to have continuity (when I should have none)between bl/w and g/w for the kill switch. I never use it anyway, is it difficult to bypass?


  2. I was following that section of the manual. The meter is to the lowest setting and I read .5 between the green terminal in the black terminal, but I cannot get a reading between the green terminal and the end of the wire, I am definitely contacting the wire out on the end… I even had an electricApprentice try it and he got the same result

    it is a 350a


  3. So, I was riding on a very hot and humid day, and the ol girl (87 fourtrax 350) suddenly stopped running.  I got it pulled home, discovered no spark. Couldn’t get an ohm reading on the secondary coil. Ordered a new one off eBay, brand new genuine Honda... hooked it up still no spark, so I took it off and brought it to the multimeter, and I’m getting out of  range reading on the primary coil but no reading on the secondary as pictured (exactly like the old coil).  Am I doing something wrong here? 

    C6CBC8C2-D79C-4EAB-9590-97447F01CFC8.jpeg

    C4CEBB2D-E563-411D-B28F-127DDC1460E8.jpeg


  4. I don’t think I ever introduced myself.  I’m keeping an ol 87 350 running with help from the forum. I’m located in central Minnesota.  I don’t have much for great places to ride around here, but I do use it for hunting/fishing.. 

    For work I do rural mail delivery, and I still do part time construction (was full time almost 20 years).  
    I have a fiancé and 6 year old daughter, and a couple dogs..
    what else is there to say, besides SKOL VIKES!!! (I see all you aints fans lol)

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  5. Well you all inspired me to do a more thorough cleaning (I noticed that one of the gaskets had been silicone at one time) and got the parts in the correct order (I am certain they were not correct the first time I took it apart).  The only thing I skimmed on is I  put it together without the baffle, because I never had one and I couldn’t seem to find a replacement.  I got it together, and the ol girl runs good again!

    thank you all

    • Like 3

  6. 9 hours ago, Goober said:

    Two other things

    the main jet is removed by pushing down on it (use the butt end of a screwdriver) from the throttle piston bore

     

    did your carb have a good passage plug?

    see the carb on the left? It’s missing one—you can see it in the carb gasket pack.

     

    52E58B3D-4B67-4960-8D4D-EF3EEC360722.jpeg

    Yes I do have the old passage plug, my kit did not come with a new one. 
    I took a picture pre-disassembly, don’t laugh too hard.. I did put it together like this, but I did not have a manual and I copied the way it was as closely as I could… I’m obviously not the first person to have been in there. 
    I seem to be missing the “baffle”, I do not have an old or new one… How important do you think that part is?

    AA8BC2B1-7F9E-49B6-863B-E0958E9CF618.jpeg

    • Like 1

  7. FOR CRYING OUT LOUD THERES A SERVICE MANUAL? Sorry for yelling but I looked through all the old posts trying not to ask for help when the information is available 🤦🏼‍♂️🤦🏼‍♂️ 
    thank you got the very thorough answers, I’ll get it together later today

    • Haha 1

  8. Well here I go again...  

    I took apart the carb to clean it, and some of the gaskets stretched, so I ordered a shindy kit. Now it’s been over a week, and I’m not certain where; the Orings, the one little washer, and that one little round seal that isn’t an oring, goes..😬

    417EDABD-DE2F-48E3-8121-29B687C05C6B.jpeg

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